MembersPage/GergelyLezsak/MyMThirty (2008-09-12 15:12:56)

my M30 turbo engine/VEMS GenBoard 3.3 build page

2008

CarsAndGirls_bmwsopron4_210.jpg

After some piston-replacement, new turbo and cam, head studs and other slight mods, the car is running again.

Problems:

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Strange voltage reading on the ECU:

http://quasar.dynaweb.hu/%7Elezsi/bmw/200808/datalog200808311613_3rd_gear_acc.xls

  • For some tests VEMS seemed to show correct values, probably real wiring issue lays behind

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My attempts to use shift-cut always ended up in engine stall even from high rpms, and serious white smoke (excess fuel in exhaust).

I'm running the same wiring, firmware version (1.1.26) and config as last year, so it's a mistery for the moment.

Did some bench-testing on same fw+conf with another ECU. Besides the function seemed to work OK generally, there are some problems here:

If shiftcut switch is ON for more than the timing for the cut, releasing of the button _sometimes_ also results in a similar cut. Log: http://quasar.dynaweb.hu/%7Elezsi/bmw/200809/desk-shiftcut-test-cut_fuel_and_spark.xls

Another problem (?) that spark cut didn't happened here, however both fuel and spark cutting were enabled. It might be related to RPM (ALS settings?), as logs at higher rpm showed spark cut:

http://quasar.dynaweb.hu/%7Elezsi/bmw/200809/desk-shiftcut-test-cut_fuel_and_spark-withALS.xls

http://quasar.dynaweb.hu/%7Elezsi/bmw/200809/desk-shiftcut-test-cut_fuel_and_spark-withALS2.xls

These made with ALS enabled, but the case is the same when it is disabled.

A config for the test: http://quasar.dynaweb.hu/%7Elezsi/bmw/200809/megasquirt200808311840.msq

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2007

normal_lezsi%20kipufogo%20007.jpg

normal_lezsi%20kipufogo%20012.jpg

2007.09.03. UPDATE

Car is mapped up to 1.5-1.7bars of boost (which is reached only in 5th gear)

Got boost control also, but not in everyday use, just preparation for dyno run planned today evening.

Knock experiments made.

Details going to be here: MembersPage/GergelyLezsak/BigSixTurbo/KnockSense

2007.07.31.

Car is mapped up to 1.2-1.3 bars of boost, probably around 450 BHP on the crank.

Can you check the wideband parameters? pumppw_zero and nernstdc_target (according to the values you got from WebShop via email, and maybe the values you had inside the ecu when shipped), and redo free-air calibration. Maybe misfire also contrinuted to the lean reading.

2007.07.14.

I had serious troubles with ECU #378: S259 and P259 outputs didn't work at all. INJFET and I259 seemed OK.

Lambda heater value on LCD didn't start to raise at MDE02 command. However later the sensor got hot somehow -not every time. Could this be a config problem?

Later I started the car with another ECU. No tuning yet.


OLD DATA

- I plan to use MembersPage/GergelyLezsak/COP ignition

- Just another option: MembersPage/GergelyLezsak/WastedSpark

- I'll need MembersPage/GergelyLezsak/CamTrigger to use them sequentially

- More to come...