History of MembersPage/GergelyLezsak/ETwentyOne
Older Newer
2008-11-04 13:55:18 . . . . MembersPage/GergelyLezsak [Blown drivers and C:R brainstorming]
2008-11-03 08:07:56 . . . . MembersPage/MattiasSandgren [Some comments about c/r, ignition and blown FET]
2008-10-31 17:38:10 . . . . MembersPage/GergelyLezsak [update and blown injector driver here too]
2007-07-30 15:59:14 . . . . MembersPage/GergelyLezsak [Config & Tables link]
2007-07-28 07:12:30 . . . . MembersPage/MarcellGal [ mcd dump needed to verify trigger settings]
2007-07-28 07:11:09 . . . . MembersPage/MarcellGal [without config it's impossible to verify]
2007-07-18 07:43:05 . . . . 194.88.59.2 [Ign Comment by Fero]
2007-07-17 12:45:48 . . . . MembersPage/GergelyLezsak [thinking about strange ign adv values]
2007-07-16 14:28:12 . . . . dsl51B63A06.pool.t-online.hu [some help]
2007-07-16 13:39:09 . . . . MembersPage/GergelyLezsak [Questions updated...]
2007-07-09 15:23:18 . . . . MembersPage/GergelyLezsak [Car started. Questions on 1.1.18 idle support and ignition]
2007-06-16 11:38:05 . . . . MembersPage/GergelyLezsak [New project page]


Changes by last author:

Changed:
** Interesting point, but hard to believe as a reason to kill an output after long normal operation, -will check connectors however.
Added:
** It was last year, but we've utilized a load of methods to check, including strobing at 0 advance (every second flash was right on the mark), checked cylinder top in sparkplug bore and counting teeth, it was really on spot and running 50degs of advance. In the range of 15-25 degrees it was very weak with normal lambda and horrible EGT (measured and seen glowing exh. headers)
Added:
** I'm using the very same trigger setup now (in 2008) with no problems after the compression has been raised significantly
Changed:
*** 6.5:1 was a calculated ratio after disassembling. Pressure measurements was slightly higher like 8 bars, can't remember exactly. However, correlation between these values is interesting, especially why it's higher than calculated?